Incident Overview

Date: Wednesday 6 November 2002
Aircraft Type: Fokker 50
Owner/operator: Luxair
Registration Number: LX-LGB
Location: 1 km NE of Niederanven – ÿ Luxembourg
Phase of Flight: Approach
Status: Destroyed, written off
Casualties: Fatalities: 20 / Occupants: 22
Component Affected: UnknownUnknown
Investigating Agency: ATIATI
Category: Accident
On August 26, 2023, Luxair Flight 9642 experienced a significant aviation incident during its flight from Berlin-Tempelhof to Luxembourg. The aircraft was cleared to descend to FL90 and then to FL180, and then to a cruising altitude of FL180. At 09:52, Frankfurt control instructed the crew to descend to FL90 and inform Luxembourg Approach of their intentions. Luxembourg Approach responded with a ‘Luxair niner six four two enter Diekirch holding at flight level niner zero it will be vectors later on for an ILS approach category two on two four.’ The flight continued to FL180, and then, at 10:01, it was cleared for a further descent to 3000 feet. At 10:04:46, the controller cleared the flight to descend further to 3000 feet. The crew subsequently discontinued the approach, reporting a need for 300 meters for the approach. The pilot then stated they needed 300 metres for the approach, and the controller responded with a directive to continue the approach. The flight continued, but at 10:04:46, the captain decided to discontinue the approach, resulting in a missed approach. The co-pilot reported a ground idle stop off. Four seconds after this statement, the Tower controller reported the RVR to be 300 metres. Immediately, the engine power was reduced to idle, and the co-pilot radioed: “Nine six four two roger so we continue.” The tower then cleared the flight to land. The gear and flaps were lowered, and the aircraft descended to 10:05:17, with the left prop blade angle changing to low pitch, causing the pilot to say “Wat ass dat.” Almost immediately, the right prop blade angle also went into low pitch. The flaps were raised several sounds and exclamations were recorded by the CVR, decreasing propeller revolutions and GPWS warnings. Both engines failed, and the Fokker aircraft descended. The airplane collided with terrain and caught fire. The causes of the accident were primarily due to a lack of preparation for the landing, initiated by unnecessary occupations resulting from an obtained RVR value that was below company approved minima, leading to an uncoordinated cockpit operation. Contributing factors included violating all applicable procedures as outlined in the operations manual, including the failure to implement a go-around. Furthermore, routine procedures were violated, and the crew’s desire to arrive at its destination may have induced a psychological state, potentially leading to deviations from standard procedures. Finally, the low reliability of the secondary stop safety device, particularly the non-application of ABSC SB F050-32-4, and the operator?s internal distribution of safety information (Fokker Aircraft B.V. – Service letter137) to the crew, did not guarantee awareness of the potential loss of secondary stop on propeller pitch control. Finally, the use of training centres and non-standardised programs may have impaired the synergy of the crew.On August 26, 2023, Luxair Flight 9642 experienced a significant aviation incident during its flight from Berlin-Tempelhof to Luxembourg. The aircraft was cleared to descend to FL90 and then to FL180, and then to a cruising altitude of FL180. At 09:52, Frankfurt control instructed the crew to descend to FL90 and inform Luxembourg Approach of their intentions. Luxembourg Approach responded with a ‘Luxair niner six four two enter Diekirch holding at flight level niner zero it will be vectors later on for an ILS approach category two on two four.’ The flight continued to FL180, and then, at 10:01, it was cleared for a further descent to 3000 feet. At 10:04:46, the controller cleared the flight to descend further to 3000 feet. The crew subsequently discontinued the approach, reporting a need for 300 meters for the approach. The pilot then stated they needed 300 metres for the approach, and the controller responded with a directive to continue the approach. The flight continued, but at 10:04:46, the captain decided to discontinue the approach, resulting in a missed approach. The co-pilot reported a ground idle stop off. Four seconds after this statement, the Tower controller reported the RVR to be 300 metres. Immediately, the engine power was reduced to idle, and the co-pilot radioed: “Nine six four two roger so we continue.” The tower then cleared the flight to land. The gear and flaps were lowered, and the aircraft descended to 10:05:17, with the left prop blade angle changing to low pitch, causing the pilot to say “Wat ass dat.” Almost immediately, the right prop blade angle also went into low pitch. The flaps were raised several sounds and exclamations were recorded by the CVR, decreasing propeller revolutions and GPWS warnings. Both engines failed, and the Fokker aircraft descended. The airplane collided with terrain and caught fire. The causes of the accident were primarily due to a lack of preparation for the landing, initiated by unnecessary occupations resulting from an obtained RVR value that was below company approved minima, leading to an uncoordinated cockpit operation. Contributing factors included violating all applicable procedures as outlined in the operations manual, including the failure to implement a go-around. Furthermore, routine procedures were violated, and the crew’s desire to arrive at its destination may have induced a psychological state, potentially leading to deviations from standard procedures. Finally, the low reliability of the secondary stop safety device, particularly the non-application of ABSC SB F050-32-4, and the operator?s internal distribution of safety information (Fokker Aircraft B.V. – Service letter137) to the crew, did not guarantee awareness of the potential loss of secondary stop on propeller pitch control. Finally, the use of training centres and non-standardised programs may have impaired the synergy of the crew.

Description

Luxair flight 9642 departed Berlin-Tempelhof at 08:40 for a flight back to Luxembourg and climbed to a cruising altitude of FL180. At 09:50 Frankfurt control cleared the crew to descend to FL90 and told them to contact Luxembourg Approach control. Contact was established at 09:52 and Luxembourg Approach replied: “Luxair niner six four two enter Diekirch holding at flight level niner zero it will be vectors later on for an ILS approach category two on two four. QNH is one zero two tree current RVR beginning two five zero on mid section two seven five, stop end two two five.”. Six minutes later the controller cleared LG9642 to descend further down to 3000 feet. At 10:01 the flight was cleared for the approach: “Luxair niner six four two turn right heading two two zero to intercept. Cleared for approach, report established on the localizer.” After passing the localizer the crew contacted Luxembourg Tower and reported being established on a runway 24 ILS approach. The tower controller then passed on the runway visual range (RVR) information, which had not changed. The crew reported that they needed 300 metres for the approach, to which the controller replied : “Nine six four two copied, uh, so continue approach I keep you advised. We didn’t have three hundred, uh, during the last, uh, time.”. The approach was continued, but at 10:04:46 the captain decided to discontinue the approach: “Yo, bon mir machen en goaround, missed approach”. The co-pilot then said: “Ground idle stop off”. Four seconds after this statement the Tower controller reported the RVR to be 300 metres. Immediately engine power was reduced to idle and the co-pilot radioed: “Nine six four two roger so we continue”. The tower then cleared the flight to land. The gear and flaps were lowered and at 10:05:17 the left prop blade angle changed from ‘normal’ to ‘low pitch’, causing the pilot to say:”Wat ass dat” (What’s that??). Almost immediately the right prop blade angle also went into low pitch. The flaps were raised several sounds and exclamations were recorded by the CVR the decrease in propeller revolutions and GPWS warnings. Both engines then failed as the Fokker descended. The airplane collided with terrain and caught fire. CAUSES: “The initial cause of the accident was the acceptance by the crew of the approach clearance although they were not prepared to it, namely the absence of preparation of a go-around. It led the crew to perform a series of improvised actions that ended in the prohibited override of the primary stop on the power levers. Contributory factors can be listed as follows: 1. A lack of preparation for the landing, initiated by unnecessary occupations resulting from an obtained RVR value, which was below their company approved minima, created a disorganisation in the cockpit, leading to uncoordinated actions by each crewmember. 2. All applicable procedures as laid down in the operations manual were violated at some stage of the approach. All this did not directly cause the accident, but created an environment whereby privately designed actions were initiated to make a landing possible. 3. Routine and the will to arrive at its destination may have put the crew in a psychological state of mind, which could be the origin of the deviations from standard procedures as noticed. 4. The low reliability of the installed secondary stop safety device that was favoured by the non-application of service bulletin ABSC SB F050-32-4. Also the mode of distribution of the safety information (Fokker Aircraft B.V. – Service letter137) to the operator as well as the operator’s internal distribution to the crews, that did not guarantee that the crews were aware of the potential loss of secondary stop on propeller pitch control. 5. The lack of harmony resulting from the use of various training centres and non-standardised programs that might have impaired the synergy of the crew.”

Source of Information

http://www.skybrary.aero/index.php/F50,_vicinity_Luxembourg,_2002http://www.skybrary.aero/index.php/F50,_vicinity_Luxembourg,_2002

Primary Cause

UnknownUnknown

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