Incident Overview

Description
The Antonov 72, chartered by Trigana and flown by an Estonian crew, departed Jayapura at 08:40 for a flight to Wamena. The flight was the third flight of eight flights planned for the day between Jayapura and Wamena. The en route part of the flight was uneventful and the pilot carried out an S-approach pattern for runway 15. Because the crew misjudged their distance to the runway they ended up being unable to decrease speed and extend flaps to landing configuration. With a high rate of descent the aircraft touched down. On touchdown the airplane bounced twice, the second and last bounce was reported to be more severe than the first one, causing the nose gear to collapse. The hydraulic system sustained damage, causing fluid to leak, which caught fire due to the friction of the aircraft on the runway. The captain applied reverse power and brakes, controlling the aircraft by using rudder inputs. The airplane decelerated with smoke emitting from the forward cargo compartment. After coming to a standstill, the loadmaster opened the airplane door taking the extinguisher, attempting to extinguish the fire. The airport fire truck could not be started, so the fire fighting personnel ran to the airplane carrying portable fire extinguishers. After twenty minutes the truck’s battery had been recharged. The fire truck then drove to the scene and extinguished the fire. The Indonesian investigation report did not contain a Probable Cause.
Source of Information
https://www.airhistory.net/info/soviet.phphttps://www.airhistory.net/info/soviet.phpPrimary Cause
Misjudgment of distance to runway during descent, leading to high rate of descent and subsequent touchdown.Misjudgment of distance to runway during descent, leading to high rate of descent and subsequent touchdown.Share on: